2014 Ford Edge Engine
Owner-reported problems and safety issues filed with NHTSA. Review common failures, severity levels, and complaint trends over time.
Complaint Timeline
Chronological view of owner reports
Three different occurrences of the engine shutting off. Twice while in park and once while stopped in a drive-thru.
Faulty Water Pump causing thousands of dollars to repair. There is a recall on same models and year my vehicle should also be on it. Stalled on hiway. Had to pay more money for tow. Repairs are more than car is worth. You have to take the top part of engine off to replace it.
The contact owns a 2014 Ford Edge. The contact stated while driving 80 MPH, the vehicle stalled. There was no warning light illuminated. The contact was able to pull over to the side of the road. The vehicle failed to restart and was towed to the residence. The vehicle was then towed to an independent mechanic, where it was diagnosed with internal water pump failure. The mechanic determined that the water pump and the head gasket needed to be replaced. The vehicle was not repaired. The dealer was not notified of the failure. The contact related the failure to an unknown recall. The manufacturer was notified of the failure and referred the contact to the NHTSA Hotline for assistance. The failure mileage was approximately 86,000.
The contact owns a 2014 Ford Edge. The contact stated that while her husband was starting the vehicle, there was an abnormal clanking sound coming from the vehicle. The contact turned off the vehicle. There were no warning lights illuminated. The vehicle had been driven the day prior without any issues. The vehicle was towed to an independent mechanic, where it was determined that the engine was blown. The contact was informed that the internal water pump had failed, and there was water inside the engine. The local dealer was not contacted. The vehicle was not repaired. The manufacturer was contacted and informed the contact that the VIN was not under recall. The contact was referred to the NHTSA Hotline to report the failure. The failure mileage was approximately 130,000.
The contact owns a 2014 Ford Edge. The contact stated that the vehicle was hesitating while driving at various speeds. The contact stated that the engine and a wrench warning lights were illuminated. The failure had become more persistent and occurred at various speeds. The contact stated that after refueling, the vehicle became idle, lost power steering functionality, and lost motive power. The vehicle was restarted and regained proper functionality. The failure was intermittent but became more persistent and occurred whether the vehicle had been refueled. The contact stated while driving 55-60 MPH, the vehicle lost motive power and several attempts were needed to restart the vehicle and continue driving. The vehicle was taken to a certified mechanic who had replaced the Oxygen sensor twice, the purge valve once, and the EVAP twice; however, the failure persisted. The manufacturer was made aware of the failure. The manufacturer referred the contact to the NHTSA Hotline to report the failure. The failure mileage was 155,000.
COOLANT LEAKING INTO ENGINE FROM FAULTY WATER PUMP CAUSING ENGINE FAILURE.
The contact owns a 2014 Ford Edge. The contact stated that while driving 45 MPH, the check engine warning light illuminated, and the vehicle overheated. The contact veered to the side of the road and allowed the vehicle to cool down. The contact then continued driving. The vehicle was taken to the dealer, where it was diagnosed that there was coolant intrusion into the engine and on the spark plugs. The dealer diagnosed that the engine needed to be replaced. The vehicle was not repaired. The manufacturer was notified of the failure, but no assistance was provided. The failure mileage was approximately 92,000. The VIN was unavailable.
Driving down the hwy, lost all acceleration. Engine still alive, had power, radio, air etc Had to coast to the side of the road. Restarted car after a few minutes and problem resolved. Took to dealer but they could not find a code. Suggested replacing throttle body as possible solution based on how often they see this.
VEHICLE REPEATEDLY HAS STALLED WHILE DRIVING. ALSO WILL SOMETIMES START WITH A ROUGH IDLE AND CHECK ENGINE LIGHT. PROBLEM IS RESOLVED IF VEHICLE IS TURNED OFF AND RESTARTED.
OIL WAS CHANGED 06/15/2019 LESS THAN ONE WEEK LATER ON 06/20/2019 WHILE TURNING FROM ONE CITY STREET ONTO ANOTHER VEHICLE LOST ALL POWER, OIL PRESSURE LOW WARNING AND OIL PRESSURE LIGHT WERE DISPLAYED. VEHICLE HAD NO POWER AND BEGAN ROLLING BACKWARD. DEPRESSED BRAKE AND TURNED OFF IGNITION, RESTARTED VEHICLE AND ALL LIGHTS WERE EXTINGUISHED. MOVED VEHICLE OUT OF TRAFFIC AND CHECKED OIL LEVEL WHICH WAS FULL. TOOK VEHICLE TO LOCAL REPAIR SHOP WHO STATED THAT THE OIL PRESSURE SENSOR WAS DAMAGED. REPLACED OIL PRESSURE SENSOR ON 06/20/2019, 2 DAYS LATER WHILE DRIVING STRAIGHT ON CITY STREET, VEHICLE LOST ALL POWER AGAIN AND OIL PRESSURE LOW WARNING AND OIL PRESSURE LIGHT CAME ON AGAIN. VEHICLE LOST ALL POWER. TURNED OFF VEHICLE AND RESTARTED, ALL LIGHTS EXTINGUISHED AGAIN. REAR BRAKE LIGHTS NO LONGER FUNCTION (UPPER ON ONE SIDE, LOWER ON OTHER) BULBS ARE NOT BLOWN AND FUSE APPEARS FUNCTIONAL.
WHILE DRIVING AT APPROX 35-40 MPH, CAR SUDDENLY LOST POWER, THE YELLOW WRENCH LIGHT LIT UP AND I WAS UNABLE TO ACCELERATE NOR MAINTAIN SPEED. I BARELY MANAGED TO GET TO SIDE OF ROAD DUE TO HEAVY TRAFFIC; THE ENGINE WAS RUNNING VERY ROUGH AND WOULDN'T SMOOTH OUT. I TURNED THE ENGINE OFF, WAITED A MINUTE BEFORE RESTARTING, THE WRENCH LIGHT WENT OFF AND ENGINE RAN NORMALLY FOR THE NEXT FEW DAYS. HOWEVER, WITHIN THE WEEK, THE SAME THING HAPPENED AGAIN.
EVERY TIME I ACCELERATE HARD TO REACH HIGHWAY SPEEDS, THE EXHAUST LEAKS INTO THE CABIN CAUSING BREATHING PROBLEMS AND DROWSINESS. THIS IS A COMMON ISSUE AND THE FORD DEALERSHIP DOES NOT SEEM TO WANT TO COVER THE COSTS OF THIS SAFETY ISSUE.
FORD EDGE WITH 58,000 MILES WAS BEING DRIVEN BY WIFE. WHILE TRAVELING AT 50-55 MILES PER HOUR, THE VEHICLE SHOWED A WRENCH ICON AND DECELERATED IMMEDIATLY TO 5MPH IN THE MIDDLE OF RUSH HOUR TRAFFIC IN THE LEFT LANE. THE LOSS OF POWER PUT THE CAR INTO LIMP MODE WHERE MY WIFE HAD TO TRY TO GET TO THE SIDE OF THE ROAD. THE IGNITION WAS TURNED OFF, THEN BACK ON AND THE CAR DROVE FINE AFTERWARDS. THE SUDDEN LOSS OF PROPULSION IS VERY SCARY ESPICALLY RIGHT AFTER DROPPING YOUR 1 YEAR OLD OFF AT DAYCARE WHO COULD HAVE BEEN IN THE CAR. WE HAVE RESEARCHED THIS AND FOUND MANY OTHER VEHICLES WITH THIS DEFECT POSSIBLY THROTTLE BODY. AFTER TURNING THE CAR OFF, ALL CODES WERE ERASED SO THE ONLY WAY TO GET THE CAR CHECKED FOR THE ISSUE WOULD BE TO STRAIGHT FROM FORD "DRIVE UNTIL THE ERROR HAPPENS AGAIN".
WHILE DRIVING 55 MPH ON THE HIGHWAY, ACCELERATOR SUDDENLY STOPPED WORKING, WRENCH LIGHT CAME ON, AND ENGINE WENT INTO LIMP HOME MODE. IT WAS VERY UNSAFE TRYING TO CROSS LANES TO GET OFF OF HIGHWAY AS CAR SLOWED VERY RAPIDLY. THIS IS THE SAME ACTION ASSOCIATED WITH THE WELL DOCUMENTED THROTTLE BODY PROBLEM FORD HAS HAD WITH OTHER MODELS. ONCE OFF THE ROAD, MOTOR WAS SHUT OFF AND RESTARTED WHICH MADE THE PROBLEM GO AWAY BUT UNFORTUNATELY ERASED ANY ERROR CODES THAT MAY HAVE BEEN GENERATED.
TL* THE CONTACT OWNS A 2014 FORD EDGE. WHILE DRIVING 65 MPH, THE VEHICLE SHOOK, THE ENGINE INDICATOR ILLUMINATED, AND THE VEHICLE STALLED. SUNNYDALE FORD IN SUNNYDALE, CALIFORNIA WAS MADE AWARE OF THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VIN WAS INVALID. THE FAILURE MILEAGE WAS APPROXIMATELY 46,000.
TL* THE CONTACT OWNS A 2014 FORD EDGE. WHILE THE ACCELERATOR PEDAL WAS DEPRESSED, THE VEHICLE HESITATED BEFORE ACCELERATING. THE VEHICLE WAS TAKEN TO ANTELOPE VALLEY FORD LINCOLN (1155 AUTO MALL DR, LANCASTER, CA 93534, (888) 483-0454). THE FAILURE COULD NOT BE DUPLICATED AND NO DIAGNOSTIC FAILURE CODES WERE FOUND. THE VEHICLE WAS NOT REPAIRED. THE CONTACT TOOK THE VEHICLE TO TWO DIFFERENT INDEPENDENT MECHANICS WHERE IT WAS DIAGNOSED THAT THERE WAS TURBO LAG. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE AND INFORMED THE CONTACT THAT THE ISSUE WAS A FUNCTION OF THE VEHICLE. THE CONTACT STATED THAT AN INSPECTOR WAS HIRED FOR A FINAL INSPECTION AND DETERMINED THAT TURBO LAG WAS THE ISSUE. NO FURTHER ASSISTANCE WAS OFFERED. THE APPROXIMATE FAILURE MILEAGE WAS 23.
UNDER HARD ACCELERATION A STRONG ODOR OF EXHAUST IS SMELLED INSIDE THE CABIN. WINDOWS UP AND MAKES NO DIFFERENCE IF A/C IS ON OR OFF OR IN THE RECIRCULATION MODE.
TL* THE CONTACT OWNS A 2014 FORD EDGE. WHILE ACCELERATING THE VEHICLE, AN EXHAUST ODOR ENTERED THE VEHICLE. THE DEALER WAS UNABLE TO DETERMINE THE CAUSE OF THE FAILURE THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE VIN WAS UNKNOWN. THE APPROXIMATE FAILURE MILEAGE WAS 37,000. UPDATED 05/31/17*LJ *CN
PURCHASED NEW 2014 EDGE IN AUGUST 2014. INCIDENT OCCURRED ON OCTOBER 18, 2015 AT 19,900 MILES. ON A CLEAR, SUNNY, SUNDAY DROVE FROM 9:00 AM NORTHWEST OF AUSTIN, TEXAS ABOUT 250 MILES WITH SEVERAL STOPS ALONG THE WAY TO 3:00 PM. ENTERING GALVESTON, TEXAS. NO PROBLEMS OF ANY KIND ALONG THE WAY. ENTERING TOWN, DRIVING STRAIGHT AND LEVEL ALONG ROAD IN CLEAR WEATHER, DRY SMOOTH ROAD ABOUT 30 MPH. ENGINE SUDDENLY QUIT - DEAD. COASTED INTO (FORTUNATE) PARKING LOT. NOTED BRIGHT RED OIL PRESSURE LIGHT CAME ON WHILE COASTING - OTHER LIGHTS ALSO BUT COULD NOT READ THEM DUE TO STRESSFUL SITUATION. CHECKED OIL LEVEL IN PARKING LOT - FULL AND NORMAL. TRIED STARTING ENGINE - STARTED RIGHT UP WITH NO PROBLEM. STARTED AND STOPPED ENGINE SEVERAL TIMES - ALL WITH NO PROBLEM. CAUTIOUSLY CONTINUED DRIVING IN GALVESTON AND RETURNED BACK TO DEALERSHIP NEAR HOME. NO FURTHER PROBLEMS WITH ENGINE. DEALERSHIP SERVICE COULD FIND NO PROBLEM AND HAD NO REAL IDEA WHAT CAUSED ENGINE TO SUDDENLY DIE WHILE DRIVING. PROBLEM HAS NOT REPEATED - YET.
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Quick Summary
The 2014 Ford Edge has 19 Engine complaints on file. Review the timeline above for detailed owner experiences.