507 complaints reported

1997 Ford F-150 Engine

Owner-reported problems and safety issues filed with NHTSA. Review common failures, severity levels, and complaint trends over time.

Reports
507
Crashes
1
Fires
42
Injuries
2

Complaint Timeline

Chronological view of owner reports

Sep 2016

STARTED THE VEHICLE IN A PARKING LOT. THE SPARK PLUG BLEW OUT OF THE HEAD ON THE PASSENGER REAR OF THE MOTOR. TRIED THE APPROPRIATE HELICOIL REPAIR KIT BUT THERE WERE NO THREADS TO TAP INTO.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Jan 2016
Jun 2016

MY FORD F150 SOMEHOW GOT WATER IN THE CYLINDER AND BENT A CONNECTING ROD AT111000 MILES.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: May 2016
Sep 2015 Fire

TL* THE CONTACT OWNED A 1997 FORD F-150. WHILE PARKED, THE VEHICLE SUDDENLY BURST INTO FLAMES. THE FIRE DEPARTMENT EXTINGUISHED THE FIRE. A FIRE REPORT WAS FILED AND NO INJURIES WERE SUSTAINED. THE VEHICLE WAS DESTROYED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 132,000. UPDATED 02/02/16*LJ *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Mar 2015
Aug 2015

WHILE DRIVING HOME FROM VACATION, WITH ABOUT 150 MILES TO GO, THE #2 SPARK PLUG BLEW OUT OF THE ENGINE. WITH ABOUT 30 MILES LEFT THE #3 SPARK PLUG BLEW OUT. CURSE OF THE FORD TRITON ENGINE

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Jul 2015
Mar 2015

I HAVE BEEN HAVING PROBLEMS WITH ENGINE OVERHEATING, HEATER TEMPERATURE WORKING INTERMITTENTLY INSIDE, MISFIRE ON ONE CYLINDER. I HAVE REPLACED THERMOSTAT, SPARK PLUGS AND WIRES, AND COILS. DIAGNOTIC CODE STILL READS MISFIRE ON ONE CYLINDER. MISFIRE IS NOT CONSTANT. AFTER RESEARCHING I FOUND OTHERS STATING THERE IS A RECALL... "RECALL # 99B20". I CAN NOT FIND A RECALL 99B20. I DID NOTICE THERE HAVE BEEN 545 OTHER COMPLAINTS CONCERNING ENGINE COOLING AND MANIFOLD O RINGS, BLOWN HEAD GASKETS ETC DUE TO FAULTY COMPONENTS. I AM ADDING MY COMPLAINT AS WELL FOR FURTHER INVESTIGATIVE ACTION, AS I FEEL THERE SHOULD BE A REAL RECALL TO FIX THIS PROBLEM/COMPLAINTS. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Feb 2015
Feb 2015

WHILE STARTING FROM A RED LIGHT, THE ENGINE BLEW A SPARK PLUG! I HAVE THE 5.4 V-8 ENGINE. FORTUNATELY THE ENGINE WAS NOT DAMAGED OR ANYTHING ELSE. I IMMEDIATELY PULLED OFF ROAD AND HAD TRUCK TOWED TO THE LOCAL FORD DEALERSHIP. REPAIRS WERE $600.00. *JS

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Feb 2015
Jan 2015 Fire

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT WHILE THE VEHICLE WAS PARKED, IT CAUGHT FIRE. THE CONTACT STATED THAT THERE WERE FLAMES COMING FROM THE ENGINE COMPARTMENT. THE CONTACT DID NOT DISCLOSE IF A POLICE REPORT WAS FILED OR NOT AND WHO EXTINGUISHED THE FIRE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 100,000. THE VIN WAS NOT AVAILABLE.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Jan 2015
Dec 2014

I CAME HOME FROM WORK ON 12/13 2014 AND NOTICED I HAD A WATER PUDDLE UNDER MY TRUCK SO ON 12/14/2014 I PULLED IN THE GARAGE AND DID SOME SEARCHING ONLY TO FIND THE OUTLET TUBE IN THE MANIFOLD WAS LEAKING I ASSUMED IT WAS THE RUBBER HOSE AND WHEN I WENT TO REPLACE IT THE OUTLET TUBE BROKE OFF AT THE BASE OF THE INTAKE MANIFOLD. UPON DOING SOME RESEARCH I FOUND THAT THE ONLY WAY TO REPLACE IT IS TO BUY A NEW INTAKE MANIFOLD SO AT THIS POINT MY TRUCK IS STUCK IN THE GARAGE . I CHECKED THE OUTLET TUBE AND FOUND 2 PINHOLES IN IT.THIS IS A CRATE MOTOR REPLACED BY FORD AT 88000 MILES I CAN'T AFFORD THE 500.00 THAT A NEW ONE WILL COSTS SO I'M OUT A VEHICLE AT THIS TIME. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Dec 2014
Sep 2014 Fire

THE TRUCK WAS PARKED IN A STRIP MALL PARKING LOT. A FEW MINUTES LATER SOMEONE SAID THAT THERE WERE FLAMES COMING FROM THE HOOD. THE CAR WAS A TOTAL IN 10 MINUTES. FOUR OFF DUTY FIREMEN WERE THERE AND COULD NOT PUT THE FLAMES OUT. NEAR BY FIRE STATION WAS CALLED. ITS RESPONSE WAS WITH IN A FEW MINUTES. TRUCK WAS TOTALED. *TR

Type: Vehicle, Vehicle: 1997 FORD F SERIES, Manufacturer: Ford Motor Company
Incident: Sep 2013
Jul 2014

MY TRUCK WAS LOOSING WATER TO THE OIL PAN AND CAUSED THE ENGINE TO NEED REPLACING IN 2004. FORD CHARGED ME 5200.00 TO REPLACE THE ENGINE AND SAID THE WARRANTY WOULD NOT COVER IT. NOW THE REPLACEMENT ENGINE IS DOING THE SAME THING. WHY WILL FORD NOT ADMIT THE PROBLEM WITH THE 97 4.2 AND NOT TRY TO COVER IT UP.? I DO NOT HAVE ALOT OF MONEY AND CAN'T AFFORD TO LET THEM KEEP FIXING THEIR PROBLEM. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: May 2004
Jan 2014 Fire

I WAS DRIVING DOWN THE ROAD. THE ENGINE GOT CAUGHT ON FIRE. WHEN I HAVE THE MECHANIC LOOKED AT IT HE SAID THAT IT LOOKED LIKE THE ROCKER ARM IN THE ENGINE CAME OFF AND HE SAID THE THAT THE VALVES GOT DESTROYED FROM THE ROCKERS. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Aug 2014
Dec 2012

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 30 MPH, THE OIL PRESSURE WARNING GAUGE ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC FOR DIAGNOSTIC TESTING. THE MECHANIC STATED THAT THE OIL PRESSURE SENSOR NEEDED TO BE REPLACED. THE CONTACT STATED THAT THE FAILURE WAS REPAIRED THREE TIMES. THE VEHICLE WAS TAKEN TO A FOURTH DEALER FOR DIAGNOSTIC TESTING HOWEVER, THE TECHNICIAN ADVISED THAT THERE WERE NO FAILURES. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND DID NOT OFFER ANY ASSISTANCE. THE VEHICLE WAS NOT REPAIRED. THE APPROXIMATE FAILURE MILEAGE WAS 103,000 AND THE CURRENT MILEAGE WAS 107,600.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Apr 2010
Sep 2012

TL* THE CONTACT OWNS A 1997 FORD F150. THE CONTACT STATED THAT AFTER STARTING THE VEHICLE, THE ENGINE FAILED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE ENGINE BLEW A ROD THROUGH THE OIL PAN. AS A RESULT, THE MOTOR CRATE NEEDED TO BE REPLACED. AFTER THE REPAIRS THE CONTACT HEARD A LOUD NOISE COMING FROM THE ENGINE AFTER STARTING THE VEHICLE. THE VEHICLE WAS NOT TAKEN TO A DEALER FOR INSPECTION. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURERER WAS MADE AWARE OF THE FAILURE WHO DID NOT OFFER ANY ASSISTANCE. THE FAILURE MILEAGE WAS 82,000.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Oct 2003
Jul 2012

FORD RECALL 99B29. FRONT COVER GASK UNABLE TO HOLD COOLANT. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Apr 2012
Jul 2012

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT WHILE DRIVING 30 MPH, A LOUD BANGING NOISE EMITTED FROM UNDER THE HOOD AND THE CHECK ENGINE LIGHT ILLUMINATED ON THE INSTRUMENT PANEL. THE FRONT END OF THE VEHICLE ALSO BEGAN TO SHAKE. THE VEHICLE WAS NOT TAKEN TO THE DEALER, BUT THE MANUFACTURER WAS NOTIFIED. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS UNKNOWN AND THE CURRENT MILEAGE WAS 211,000.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: May 2011
Jun 2012

4.2L F150 HAD A SLOW LOSS OF COOLANT AND NOT BEING NOTIFIED THAT THIS COULD BE A POTENTIAL PROBLEM WHICH COULD LEAD TO ENGINE DESTRUCTION, I WOULD SIMPLY ADD MORE COOLANT. THIS CONDITION RESULTED IN COMPLETE HYDRO LOCK AND DESTROYING #5 ROD BEARING. WHILE I CAN WELL UNDERSTAND PROBLEMS ASSOCIATED WITH VEHICLES OF 1997 VINTAGE I CAN NOT UNDERSTAND AT ALL FORD NOT ADVISING CONSUMERS OF POTENTIAL PROBLEMS WITH THEIR VEHICLES BEFORE THEY SPEND 4K$ IN REBUILDING AND INSTALLING THIS LONG BLOCK AND FINDING OUT THEY HAD SQUANDERED THEIR MONEY ON TRYING TO RESURRECT A DEAD HORSE WITH 86069 MILES ON THE ODOMETER. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Feb 2012
Apr 2012

WHEN I FIRST BOUGHT THE TRUCK IN 2001, THE ENGINE HAD APPROXIMATELY 82K MILES. I WAS HAVING A HARD TIME STARTING AND SOMETIMES IT WOULD NOT START. AT FIRST THE DEALER THOUGHT IT WAS THE STARTER AND THEY REPLACED IT. THEY TOLD ME TO TAKE IT TO PEPBOYS TO GET THE STARTER REPLACED. WHEN THEY STARTED THE CAR A MASS OF GRAY SMOKE COME OUT OF THE TAIL PIPE. TWO DAYS LATER THE ENGINE FROZE. SINCE I HAD A WARRANTY AGREEMENT I TOOK THE TRUCK TO A LOCAL FORD DEALER, THEY STATED IT HAD HYDROLOCKED AND THE ENGINE NEEDED TO BE REPLACED. THE WARRANTY COMPANY SENT OUT A SHORT BLOCK AND FORD COMPLETED THE REST OF THE REPAIRS. AT THE BEGINNING OF APRIL, MY DAUGHTER WAS USING MY TRUCK AND SHE DROVE IT TO MY HOUSE AND PARKED IT OUT FRONT. IT SAT FOR 2 WEEKS, WHEN I WENT TO START IT, IT WOULD NOT TURN OVER. REPLACE THE BATTERY AND IT STILL WOULD NOT TURN OVER. AT THAT TIME THE STARTER SMOKED AND TOOK THE TRUCK TO A MECHANIC WHO REPLACED THE STARTER. HE TRIED TO TURN IT OVER AND IT WOULD NOT TURN. HE STATED THEY TRIED USING A TORQUE WRENCH AND STILL COULD NOT TURN THE MOTOR. THE MECHANIC RECOMMENDED THAT THE ENGINE BE REPLACED. I HAD THE TRUCK TOWED TO MY HOME. AFTER READING THE INFO ABOUT ANOTHER TRUCK HYDROLOCKING, I DECIDED TO CHECK TO SEE IF MY TRUCK HAD THE SAME PROBLEM. WHEN I PULLED THE PLUGS, I HAD COOLANT DRAIN FROM THE #3 CYLINDER AND A SMALL AMOUNT OF COOLANT LEAK FROM #5 CYLINDER. PREPARING TO REPLACE THE LOWER AND UPPER INTAKE MANIFOLD GASKETS. *TR

Type: Vehicle, Vehicle: 1997 FORD F SERIES, Manufacturer: Ford Motor Company
Incident: Mar 2012
Apr 2012

TRUCK HAS A 4.2 LITER, V-6 ENGINE. A WEEK PRIOR TO INCIDENT THE TRUCK WAS DRIVEN THEN PARKED IN A MY GARAGE. ON THE INCIDENT DAY I TRIED TO START THE TRUCK BUT HEARD ONLY A LOUD, HARD KNOCK WHEN THE STARTER ENGAGED. THE ENGINE WOULD NOT TURN OVER. THE BATTERY VOLTAGE CHECKED OUT OK. I HAD THE TRUCK TOWED TO A LOCAL REPAIR SHOP. THE STARTER WAS REMOVED AND CHECKED OUT OK ELECTRICALLY. THE MECHANIC MANUALLY ROTATED THE ENGINE BACKWARD 1-1/2 TURNS (HE COULD NOT ROTATE IT FORWARD) THEN TRIED TO START IT BUT THE ENGINE AGAIN MADE A LOUD, HARD KNOCK SOUND. THE MECHANIC THOUGH THE TIMING CHAIN FAILED OR A PUSH ROD WAS BENT. HOWEVER, SINCE THE TRUCK RAN FINE THE LAST TIME IT WAS USED I FELT THE PROBLEM DEVELOPED DURING ITS LAST USE AND LAST COOLDOWN. I CONCLUDED A GASKET FAILED (OR A HEAD CRACKED) ALLOWING COOLANT TO LEAK INTO ONE OR MORE CYLINDERS DURING ITS LAST COOLDOWN. I HAD THE TRUCK TOWED BACK TO MY GARAGE. I REMOVED ALL SPARK PLUGS AND FOUND COOLANT DRAINING FROM THE PASSENGER SIDE FRONT CYLINDER WHICH WAS CAUSING HYDROLOCK. I ROTATED THE ENGINE BACKWARD 4-1/2 TURNS THEN FORWARD 9 TURNS. THE ENGINE NOW TURNED FREELY. A TOTAL OF 4 TO 6 OUNCES OF COOLANT CAME OUT OF THE CYLINDER. I SPOKE WITH A MECHANIC WHO CHECKED THE FORD ALERT SYSTEM AND FOUND A POSTING FOR THE 1997 4.2L V-6 ENGINES THAT INDICATED THEY ARE PRONE TO INTAKE MANIFOLD O-RING FAILURES. I FOUND MANY REPORTS OF SIMILAR FAILURES FOR THIS YEAR AND ENGINE TYPE. I INTEND TO CHECK IN WITH THE LOCAL FORD DEALERSHIP TO GET THEIR TAKE ON THIS PROBLEM AND FIND OUT WHY I WASN'T NOTIFIED ABOUT A "RECALL". *JS

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Oct 2012
Mar 2012 Fire

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT AFTER PARKING THE VEHICLE, HE HEARD THE HORN SOUNDING OFF. THE VEHICLE ENGULFED INTO FLAMES SOON THEREAFTER. THE FIRE DEPARTMENT WAS NOTIFIED AND EXTINGUISHED THE FLAMES. THE FIRE CHIEF STATED THAT THE FRONTAL AREA ON THE DRIVER'S SIDE WAS THE CAUSE OF THE FIRE. THE VEHICLE HAD NOT BEEN INSPECTED. THE MANUFACTURER WAS NOTIFIED AND OFFERED NO ASSISTANCE. THE FAILURE MILEAGE WAS APPROXIMATELY 161,000. THE VIN WAS UNAVAILABLE.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Mar 2012
Mar 2012 Fire

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT THE VEHICLE CAUGHT ON FIRE WHILE PARKED. NO ONE WAS INJURED FROM THE FIRE. THE FIRE DEPARTMENT WAS CONTACTED TO EXTINGUISH THE FIRE. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE AND TOOK A COMPLAINT. THE CONTACT DID NOT KNOW WHAT CAUSED THE FIRE. THE FAILURE MILEAGE WAS 200,000.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Mar 2012
Feb 2012 Fire

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STATED THAT AFTER PARKING THE VEHICLE, FLAMES EMITTED FROM THE ENGINE COMPARTMENT. THE CONTACT MENTIONED THAT HE WAS ABLE TO EXTINGUISH THE FIRE WITH A WATER HOSE. THE FIRE DEPARTMENT WAS NOT CONTACTED AND NO INJURIES WERE REPORTED. THE VEHICLE WAS NOT TAKEN TO THE DEALER FOR INSPECTION OR REPAIRS. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE AND THE CURRENT MILEAGE WAS 207,000.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Apr 2011
Jan 2012

ENGINE FRONT COVER GASKET FAILED IN LINE WITH RECALL 99B29. FORD DOES NOT INCLUDE MY TRUCK BUILT 1997 IN RECALL CAMPAIGN INDICATING THE ORIGINAL RECALL HAS BEEN INADEQUATE. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Jan 2012
Sep 2011

FRONT DRIVERS SIDE SPARK PLUG BLEW OUT OF ENGINE AND DESTROYED COIL PACK RIPPING THE THREADS OUT OF THE HEAD. *TR

Type: Vehicle, Vehicle: 1997 FORD F SERIES (LIGHT), Manufacturer: Ford Motor Company
Incident: Mar 2011
Aug 2011

TL* THE CONTACT OWNS A 1997 FORD F-150. THE CONTACT STARTED THE VEHICLE AND A SPARK PLUG EJECTED FROM THE HEAD OF THE ENGINE. THE CONTACT SHUT THE VEHICLE OFF AND HAD THE VEHICLE TOWED TO A LOCAL MECHANIC. THE LOCAL MECHANIC CONFIRMED THE BLOWN SPARK PLUG AS WELL AS A COIL, AND ADVISED REPLACING THE ENGINE. THE CONTACT CALLED THE MANUFACTURER TO ORDER THE NECESSARY PARTS FOR REPAIRS AND THE MANUFACTURER ADVISED THAT THERE WERE ONLY TWO ENGINE HEADS AVAILABLE IN THE COUNTRY. THE VEHICLE WAS NOT REPAIRED. THE CONTACT BELIEVED THE VEHICLE TO BE UNSAFE TO DRIVE. THE FAILURE MILEAGE WAS 100,000. THE VIN WAS NOT AVAILABLE.

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Aug 2011
May 2011

JUST DRIVING MY 1997 FORD F-150 AND HAVE HAD 2 SPARK PLUGS FLY OUT THE TRUCK. MOTOR THEN RUNS ROUGH AND CONTINUES TO OPERATE FOR SOME TIME BEFORE YOU GET ANY ENGINE LIGHT. AFRAID TO LET WIFE USE TRUCK CAUSE IT COULD CATCH FIRE. *TR

Type: Vehicle, Vehicle: 1997 FORD F-150, Manufacturer: Ford Motor Company
Incident: Oct 2011

Trend Over Time

Complaints by year

Quick Summary

The 1997 Ford F-150 has 507 Engine complaints on file. 1 crashes have been reported. Review the timeline above for detailed owner experiences.