1993 Ford F-250 Engine
Owner-reported problems and safety issues filed with NHTSA. Review common failures, severity levels, and complaint trends over time.
Complaint Timeline
Chronological view of owner reports
WHILE TRAVELING NOTICED NOISE COMING FROM VEHICLE. DEALER STATED EXHAUST SYSTEM MUFFLER WAS BENT. PLEASE PROVIDE FURTHER INFORMATION. *AK
WHILE TRAVELING NOTICED NOISE COMING FROM THE VEHICLE. DEALER STATED EXHAUST SYSTEM MUFFLER WAS BENT. PLEASE PROVIDE FURTHER INFORMATION. *AK
WHILE DRIVING STARTED SMELLING EXHAUST FUMES INSIDE VEHICLE. DRIVER STARTED GETTING A HEADACHE. TOOK VEHICLE TO DEALER & MECHANIC NOTICE BOLTS ON MOTOR SHEARED OFF ATTACHMENT. PROBLEM REPAIRABLE, BUT WILL REAPPEAR DUE TO DESIGN OF BOLTS. MANUFACTURER KNOWS OF PROBLEM. *AK
THE VEHICLE HAS HAD CONTINUED PROBLEMS WITH ENGINE KNOCKING, THE DEALERSHIP WILL TEMPORARILY FIX THE PROBLEM BUT THEN IT RETURNS. *MJS
SERVICE BULLETIN 95-5-24 WAS SENT TO ME 9 TO 12 MONTHS AGO ON A COOLING SYSTEM ADDITIVE TO ADD TO MY SYSTEM TO PREVENT CORROSION OF THE BLOCK AND EATING THROUGH THE CYLINDER WALLS. I ADDED THE REQUIRED AMOUNT OF THIS ADDITIVE, AND HAVE NOT GIVEN IT MUCH THOUGHT UNTIL MY ENGINE SEIZED UP. WHEN THE ENGINE WAS TORN DOWN IT WAS FOUND TO BE CAUSED BY PIN HOLES THROUGH THE CYLINDER WALLS WHICH LET COOLANT WASH DOWN THE CYLINDER WALLS AND CAUSED THE ENGINE TO SEIZE AND BEND A ROD. CURRENTLY THE ENGINE IS APART UNTIL I CAN FIGURE OUT WHAT TO DO. FORD TOLD ME THAT EVENTHOUGH THEY DESIGNED A FAULTY SYSTEM, THAT THEY DO NOT HAVE TO DO ANYTHING, AND THAT IS WHY I AM SENDING THIS TO YOU. ALSO THE BULLETIN CAME OUT IN 95 AND I NEVER RECEIVED A COPY UNTIL LATE 97. I WISH I STILL HAD A COPY OF THE BULLETIN. HOPE YOU CAN HELP!
POROUS BLOCK DUMPED WATER INTO CYLINDARS
IDLER PULLEY/TENSIONER AND SERPENTINE BELT FAILED SEVERAL TIMES AFTER RECALL REPAIR WORK CAUSING LOSS OF BRAKING CONTROL.
ON SEVERAL OCCASIONS THE SERPENTINE BELT BROKE, CAUSING OTHER COMPONENTS TO FAIL AS WELL, RESULTING IN LOSS OF CONTROL.
WHILE DRIVING VEHICLE ABOUT 55-60 MPH THE SERPENTINE BELT CAME OFF AND THE VEHICLE LOST POWER STEERING AND BRAKES. DRIVER WAS ABLE TO PULL TO THE SIDE OF THE ROAD SAFELY WHEN GEARING THE TRUCK DOWN AND APPLYING THE EMERGENCY BRAKE. *AK
THE ENGINE ELECTROLYSIS BETWEEN WATER & DIESEL, MADE HOLES IN CYLINDER WALLS FROM INSIDE OUT. IT HAD RUINED THE ENGINE. *AK
PREVIOUS RECALL ISSUED BY MANUFACTURER REGARDING EXCESSIVE WEAR OF THE DRIVE BELTS WHICH INCORPORATES WITH THE POWER STEERING PUMP AND BRAKES. THIS COULD RESULT IN A LOSS OF CONTROL WITHOUT PRIOR WARNING. THIS IS THE FOURTH REPLACEMENT. *AK
SERPENTINE BELT BRACKET DESIGN CAUSES SERPENTINE BELTS TO FAIL.
WHEN DRIVING THE VEHICLE THE FAN BELT COMES OFF THE VEHICLE. TT
THE SERPENTINE BELT FALLS OFF AND CAUSES LOSS OF STEERING AND FAILURE OF THE POWER ASSISTED BRAKES. PLEASE DESCRIBE. *AK
SERPENTINE BELT FAIL PREMATURELY DUE TO DESIGN FLAW, FIXED BY NEW BRACKETS/TENSIONER. *DSH
THE SERPENTINE BELT CAME OF, CAUSING LOSS OF POWER. TT
RADIATOR FAN BELTS RIPS AND CAUSES ENGINE FAILURE. *AK
BEARING ON CRANKCASE WENT OUT AND ENGINE BLEW UP. PLEASE GIVE MORE DETAILS. TT
WHILE DRIVING, AT APPROX. 15MPH PULLEY BRACKETS SHREDS SERPENTINE BELT AND CAUSES TO BREAK, RESULT LOSS OF POWER AND CONTROL OF VEHICLE. TT
PULLEY BELT MAKING A LOT OF NOISE, POSSIBLE AT RISK OF POPPING. TT
SERPENTINE BELT TENSIONER BRACKET CRACKS, CAUSING BELT TO WEAR UNEVENLY. *AW
Trend Over Time
Complaints by year
Other Issues
Common problems reported
Quick Summary
The 1993 Ford F-250 has 21 Engine complaints on file. Review the timeline above for detailed owner experiences.